MembersPage/Sascha/BMWEthirty (2008-10-30 09:11:18)
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Dave's BMW E30 Turbo


Started out as an 1988 BMW E30 327i (stroker using super ETA bottom end, with a 325i head), stock everything else for now.

While N/A:

Using a VEMS V3.3 ECU, stock 60-2 wheel and CLT temp sensor, IAT from a VW, and a TPS from a 5/7 series automatic BMW. Using original engine wire harness.

Running 19# high-z injectors.

ECU running Firmware version 1.0.71


Update May. 22 2008

The BMW is now turbo. I decided to remake the entire wiring harness for the motor. The old harness was pulled and stripped down to the bare minimum for the remaining functions (starter, alt, clt gauge for cluster, etc). A new engine harness was then made with all necessary (and new) options.


Went and did some tuning and came back with... 374whp @ 18psi on 91 octane (on a very hot and humid day)

357rfj9.jpg


Sept 18 2008 - Injector driver issue

Having major problems with the ECU! Two days ago injector driver 1 blew. Just today injector driver 6 went. The car runs fine. The tune hasn't been changed at all. What could be causing random injector drivers to fail like this?


Oct. 17 2008 - Injector drivers are randomly blowing again

So we decided to connect to another input on ch 7 - EC18-12 with a clean ground for pull down, using a 2K4 5V pull up as usual. Everything was fine (LC working, car running strong) for about 2 weeks. Now just today again Cyl. no. 2 injector driver blew. The car was being driven hard but LC was not being used at all or at anytime during the day.

I'm starting to wonder if there is a problem with the ECU, or a setting for the injectors?

PWMing is disabled due to the use of TS diode. Maybe there is an issue using the TS diode with the old high power/PWM flyback setup?

What do I need to check? I will upload the config tomorrow for review, but I highly doubt there is an issue in the config as nothing has changed in the ECU (FW, CONFIG and TABLES are all the since ever since the car was started and tuned on the 630cc injectors well over 10 months ago).

The problems with the injector drivers only started to show up approx. 1 month ago.

Any other suggestions on what I can check?

  • CHECK YOUR ANALOG GROUND! CHANGE THE WIRE. THAT WILL BE THE PROBLEM!- I MEAN CHANGE THE GROUND WIRE OF THE EC36 PIN26 FOR A NEW ONE!!! --FERO
  • I did change it... the last time you told me to... This is a new/clean ground wire for the pulldown. And like I said the LC wasn't used at all that day or when it happened. Which means the ground signal wasn't going to the ECU. We are using a different switch as well.
  • The LC grounding does not makes a sense here. But if the grounding of the EC36 pin26 is bad, than you'll blew off the FETs. So you have to recheck that wire, or simply change it to a new one! --FERO
  • Wellw hat I've done for now is disconnect the pulldown for the LC. And I will inspect and change the ground for EC36-26, it is possible maybe the crimp/wire is bad. I already had this with the primary VR trigger (and this was a unterminated harness from the webshop). Thanks for the help! I will post my findings :)
  • I had the same problems,but no so often as you,car runs fine for few month and then inj. FET blows up...everything else works just fine...i dont know what is causing inj. drivers to blow...