Car is Audi S4 Avant with AAN engine.
Rst
The car works and no trigger errors has been recorded so far (driven for about 150km). The problem was that i am using Fidanza ALU flywheel. It has to small trigger for the VR sensor. It has to be bigger. Second thing were the bolts on the flywheel that hold the toothed to the flywheel. These bolt are made for regular steel. These must be changed to stainless steel or smth else that dosent react to magnet.
Also the hall sensor (near the firewall) must be in it's original markings.
After doing these little "improvments" the car started.
Now it needs to be tuned correctly and then i can enjoy my car. :) Let's see how much power and torque will the holset HX40Super give my dailydriver.
'''relevant
- what is the history of the controller ?
- Is it an econoseal or motronic55 ?
- Serialnr ?
- With what options was it ordered ?
- nr of IGBTs ?
- what modifications were done ?
- besides the home-installed AudiTrigger/CamHALLInverter)..
- ... ?
- Did the engine work before ?
- How are you sure that the used ign outputs are logiclevel ?
- Do the ign outputs (when power output stages are disconnected) measure -12V when measured from +12V as a base ? (ign on, but engine off)
We will verify your ign outputs when we see ign outputs in your config+tables ( h[2] )
- I see the wiring http://gph.planet.ee/vems/RST/ but that's just one half of the story
The ignition can be spark-tested with Man mdn00 mdn04 mdn03 mdn02 mdn01 (also from the ignition outputs dialog in new VemsTune).
- For all high-voltage ignition ("ign transformer secondary") wires make sure there is return path to engine head, eg. sparkplug thread touches ground.
- Don't electrocute yourself or the controller.
- Car doesn't start. it gives something like 5 misfires for 6-10 sec starting.
- When I tried without HALL inverter the engine gave some backfires but still not started.
- If the HALL signal and Flywheel triger wasn't aligned correctly the engine sometimes started.
The setup uses HALL trigger from distributor. The HALL signal is inverted. (home-installed AudiTrigger/CamHALLInverter).
Measure voltage BEFORE and AFTER the inverter (during cranking)
- I measured it with scope and it's ok.
The trigger_tooth=08 is good for
- factory HALL window position WITHOUT camHALL inverter
- or HALL window 180 camdegrees offset, WITH camHALL inverter
- Marcell has such setup working on his 3B. Note that ignout=cyl5 cyl4 cyl2 cyl1 cyl3 ... applies for that !
We MUST see your ignition output configuration as well (and reference trigger tooth array). Publish the mct dump (the tables are best, make a screenshot at a minimum)
- The wiring diagram is on the link: http://gph.planet.ee/vems/RST/
Config:
primep=DC
primep_temp_scaling=33
cwl=8C
cwh=23
cranking_thres=03
awev=AA
awev_temp_scaling=26
awec=22
warmup_clt_range[0]=00
warmup_clt_range[1]=00
warmup_clt_range[2]=04
warmup_clt_range[3]=18
warmup_clt_range[4]=50
warmup_clt_range[5]=64
warmup_clt_range[6]=78
warmup_clt_range[7]=8B
warmup_clt_range[8]=A6
warmup_clt_range[9]=D4
warmup_clt[0]=96
warmup_clt[1]=91
warmup_clt[2]=8C
warmup_clt[3]=46
warmup_clt[4]=3C
warmup_clt[5]=32
warmup_clt[6]=23
warmup_clt[7]=14
warmup_clt[8]=0F
warmup_clt[9]=05
warmup_rpm_scale=4D
req_fuel=27
divider=01
alternate=04
injopen=00
battfac=22
kpafac=D0
kpaoffs=8B
injocfuel=01
injrampup_battfac=FF
injpwm=FF
injpwmt=FF
als_launch_input=CF
rpmk[0]=09
rpmk[1]=60
tpsdot_kpadot_conf=00
tpsdotrate[0]=02
tpsdotrate[1]=0A
tpsdotrate[2]=13
tpsdotrate[3]=1D
tpsaq[0]=01
tpsaq[1]=02
tpsaq[2]=03
tpsaq[3]=04
als_cut_mintps=FF
tpsasync=0A
acmult=AA
tpsacold=0A
launch_enrich=00
launch_retard=00
overrun_fuelcut=1C
overrun_fuelresume=1B
rev_limit=43
airden_ignore=64
config11=41
config12=40
config13=02
batt_cal=C0
fastidle=C6
als_max_cut=00
dbaro=0A
tps_low=18
tps_high=E6
fan_temp=EA
fan_hyst=05
fan_channel=FF
iac_step_seq=D8
iac_conf=5A
iac_max_steps=1E
iac_tps_thres=03
iac_cold_idle_temp=7E
iac_warm_idle_temp=B4
iac_cold_rpm=78
iac_warm_rpm=50
iac_cold_start_pos=FF
iac_warm_start_pos=80
iac_afterstart_rpm=1E
iac_afterstart_duration=32
iac_speed=01
iac_kp=2A
iac_ki=16
iac_kd=0A
launch_rpm=FF
iac_integral_limit_dec=0A
iac_integral_limit_inc=14
iac_integral_deadband=0A
iac_deadband=0A
als_cut_maxtps=FF
iac_overclose_interval=C8
iac_ref_pos[0]=BF
iac_ref_pos[1]=BA
iac_ref_pos[2]=8C
iac_ref_pos[3]=70
iac_ref_pos[4]=6E
iac_ref_pos[5]=6B
iac_ref_pos[6]=69
iac_ref_pos[7]=66
iac_ref_pos[8]=61
iac_ref_pos[9]=57
iac_sol_channel=60
iac_ign_slope=18
softrpm_range=32
iac_ign_advance_limit=30
iac_ign_retard_limit=18
iac_ign_threshold=0C
ego_conf=06
ego_lag=04
ego_coolant=7E
ego_maxtps=E6
ego_maxmap=78
ego_minrpm=14
ego_maxrpm=46
ego_warmup=14
ego_lean_limit=03
ego_rich_limit=03
ego_pid_kp=1E
als_enrich=00
ego_delta=03
ego_target=19
ego_pid_window=01
wbo2_warmup_ramp=FF
als_react_tps=FF
wbo2_abs_limit=E0
wbo2_limit_maxt=F0
wbo2_fallback=70
wbo2_retry_t=06
als_retard_rpm1=FF
als_retard_rpm2=FF
wbo2_ri_target=A5
wbo2_nernstdc_target=86
wbo2_pump_pw_zero=67
wbo2_calibration=C3
wbo2_heater_pid_kp=45
wbo2_heater_pid_ki=11
wbo2_heater_pid_kd=1A
wbo2_heater_pid_ilimit=80
wbo2_pump_pid_kp=15
wbo2_pump_pid_ki=4E
wbo2_pump_pid_kd=00
wbo2_pump_pid_ilimit=FF
wbo2_ri_confidence_scale=80
knock_chan=01
knock_sampling_window=F2
knock1_frequency=29
knock1_gain=00
knock1_integrator=0F
knock2_frequency=29
knock2_gain=00
knock2_integrator=0F
knock_threshold=0A
knock_noise_scale=AA
knock_max_retard=50
knock_default_retard=08
knock_retard_step=04
knock_retard_delay=30
knock_advance_step=01
knock_advance_delay=50
knock_minrpm=0A
knock_maxrpm=4C
ve_learn_coolant=CF
ve_learn_max_power=64
ve_learn_rpm_scale=28
ve_learn_kpa_scale=28
ve_learn_ego_scale=50
ve_learn_min_weight=14
ve_learn_speed=32
ve_learn_limit=80
ve_learn_conf=00
lcd_c0=FE
lcd_delay=42
lcd_backlight=FF
kpa_conf=22
als_igncut_rpm2=FF
als_retard_mintps=FF
als_retard_maxtps=FF
lcd_default_view=02
primary_trigger=43
secondary_trigger=19
tooth_wheel=5A
trigger_tooth=08
another_trigger_tooth=12
crank_minper=33
tooth_wheel_twidth1=20
tooth_wheel_twidth2=00
cam_sync_r_edge_phase=00
cam_sync_f_edge_phase=00
reset_engphase_after=40
ign_tdcdelay=84
ign_dwell14=C3
ign_dwell6=38
ign_crank_advance=30
ign_out=70
ignchmax=04
engine_off_delay=04
pump_on_mintime=06
fuelpump_channel=70
inj_stage2_rate=FF
inj_stage2_start_tps=FF
inj_stage2_start_map=FF
als_igncut_rpm1=FF
als_deact_time=00
als_deact_egt=00
als_retard=CC
als_rev_limit=FF
misc1out_minrpm=00
misc1out_maxrpm=0C
misc1out_mintps=4D
misc1out_maxtps=FF
misc1out_minmap=00
misc1out_maxmap=64
misc1out_channel=7F
misc2out_minrpm=FF
misc2out_maxrpm=FF
misc2out_mintps=FF
misc2out_maxtps=FF
misc2out_minmap=FF
misc2out_maxmap=FF
misc2out_channel=FF
act_wot_rpm=FF
act_wot_channel=FF
act_rpm_rpm=FF
act_rpm_channel=FF
egt1_cal=4B
als_tks_channel=FF
boost_conf=61
boost_targetoffs=00
boost_minpressure=36
boost_pid_kp=FE
boost_pid_ki=64
boost_pid_kd=1F
boost_pid_ilimit=6E
boost_channel=50
water_pump_temp=00
hybrid_rpm_a=00
hybrid_rpm_m=00
water_pump_hyst=7E
water_pump_channel=FF
toothrel_normal=76
toothrel_missing=00
fuelcut_min_kpa=08
fuelcut_max_kpa=8C
tach_channel=17
tach_div=11
shiftcut_conf=00
shiftcut_channel=FF
shiftcut_time=7F
softrpm_rpm=3E
...
Tables missing !! We need that to verify ignition outputs.