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IMPORTANT: enter the case-INsensitive alphabetic (no numbers) code AND WRITE SOME SHORT summary of changes (below) if you are saving changes. (not required for previewing changes). Wiki-spamming is not tolerated, will be removed, so it does NOT even show up in history. Spammers go away now. Visit Preferences to set your user name Summary of change: Installing Vems3.3 on a Volvo 244 with a B21ET engine. Taken out the dreadful K-jetronic to get complete control. This car should be competing this year in the Benelux Driftseries. My name is Jochen aka Brickdrifter and I'm living in Belgium. http://img273.imageshack.us/img273/9224/img86538ys.jpg ---- '''Trigger-log''' [http://www.driftingforlife.com/images/picsjustforme/TriggerlogMexrp.zip new triggerlog zip file] evaluation pls '''2-09-06''' current setup: B21ET Ford brown top injectors Fuel pressure regulator (set to 2.5 bar) Gr.A .60/.63 trim turbo XS Power intercooler Vems controls only injection! (for now) 36-1 trigger wheel with Ford VR sensor IAT sensor from webshop Volvo 960 TPS sensor 1.0.36 Firmware Megatune, no LCD :-( We will try to get the serial connections to work properly and download the actual firmware and config. Check groundconnections and achieve a triggerlog to analyse. Follow the instructions on InputTrigger/TriggerLog, for sure the terminal outputs "garbage" that needs to be formatted for evaluation. <code> primep=00 primep_temp_scaling=80 cwl=B9 cwh=4B cranking_thres=03 awev=0A awev_temp_scaling=99 awec=2A warmup_clt_range[0]=00 warmup_clt_range[1]=00 warmup_clt_range[2]=00 warmup_clt_range[3]=14 warmup_clt_range[4]=50 warmup_clt_range[5]=64 warmup_clt_range[6]=78 warmup_clt_range[7]=8C warmup_clt_range[8]=AA warmup_clt_range[9]=C8 warmup_clt[0]=B4 warmup_clt[1]=AC warmup_clt[2]=AB warmup_clt[3]=AA warmup_clt[4]=A0 warmup_clt[5]=96 warmup_clt[6]=8A warmup_clt[7]=7A warmup_clt[8]=6E warmup_clt[9]=64 warmup_rpm_scale=BF req_fuel=2A divider=02 alternate=01 injopen=1F battfac=13 kpafac=96 kpaoffs=F6 injocfuel=20 injrampup_battfac=FF injpwm=33 injpwmt=FF injpwm6=33 rpmk[0]=0B rpmk[1]=B8 tpsdot_kpadot_conf=00 tpsdotrate[0]=06 tpsdotrate[1]=1A tpsdotrate[2]=66 tpsdotrate[3]=FF tpsaq[0]=19 tpsaq[1]=20 tpsaq[2]=2D tpsaq[3]=64 als_cut_mintps=FF tpsasync=06 acmult=00 tpsacold=78 launch_enrich=00 launch_retard=0D overrun_fuelcut=4D overrun_fuelresume=37 rev_limit=46 airden_ignore=00 config11=31 config12=40 config13=02 batt_cal=BD fastidle=C6 als_max_cut=00 dbaro=0C tps_low=26 tps_high=F5 fan_temp=00 fan_hyst=00 fan_channel=0F iac_step_seq=C9 iac_conf=40 iac_max_steps=FF iac_tps_thres=08 iac_cold_idle_temp=90 iac_warm_idle_temp=0C iac_cold_rpm=78 iac_warm_rpm=5C iac_cold_start_pos=E6 iac_warm_start_pos=D9 iac_afterstart_rpm=0F iac_afterstart_duration=96 iac_speed=32 iac_kp=14 iac_ki=0F iac_kd=1E launch_rpm=FF iac_integral_limit_dec=32 iac_integral_limit_inc=8C iac_integral_deadband=14 iac_deadband=0A als_cut_maxtps=00 iac_overclose_interval=80 iac_ref_pos[0]=BF iac_ref_pos[1]=B3 iac_ref_pos[2]=A6 iac_ref_pos[3]=99 iac_ref_pos[4]=8C iac_ref_pos[5]=80 iac_ref_pos[6]=73 iac_ref_pos[7]=66 iac_ref_pos[8]=59 iac_ref_pos[9]=4D iac_sol_channel=FF iac_ign_slope=20 softrpm_range=04 iac_ign_advance_limit=08 iac_ign_retard_limit=08 iac_ign_threshold=08 ego_conf=06 ego_lag=05 ego_coolant=B4 ego_maxtps=CC ego_maxmap=FF ego_minrpm=0C ego_maxrpm=28 ego_warmup=3C ego_lean_limit=26 ego_rich_limit=05 ego_pid_kp=28 als_enrich=00 ego_delta=33 ego_target=19 ego_pid_window=FF wbo2_warmup_ramp=C0 als_react_tps=00 wbo2_abs_limit=F5 wbo2_limit_maxt=A0 wbo2_fallback=60 wbo2_retry_t=06 wbo2_edgetime_corr=00 wbo2_edgetime_min=50 wbo2_ri_target=9A wbo2_nernstdc_target=89 wbo2_pump_pw_zero=64 wbo2_calibration=FE wbo2_heater_pid_kp=46 wbo2_heater_pid_ki=10 wbo2_heater_pid_kd=1A wbo2_heater_pid_ilimit=80 wbo2_pump_pid_kp=20 wbo2_pump_pid_ki=37 wbo2_pump_pid_kd=00 wbo2_pump_pid_ilimit=F5 wbo2_ri_confidence_scale=80 knock_conf=01 knock_sampling_window=FF knock1_frequency=29 knock1_gain=3F knock1_integrator=1F knock2_frequency=29 knock2_gain=3F knock2_integrator=1F knock_threshold=FF knock_noise_scale=FF knock_max_retard=00 knock_default_retard=00 knock_retard_step=00 knock_retard_delay=00 knock_advance_step=00 knock_advance_delay=00 knock_minrpm=FF knock_maxrpm=FF ve_learn_coolant=B4 ve_learn_max_power=FF ve_learn_rpm_scale=1E ve_learn_kpa_scale=1E ve_learn_ego_scale=43 ve_learn_min_weight=4D ve_learn_speed=FF ve_learn_limit=FF ve_learn_conf=00 lcd_c0=FE lcd_delay=FF lcd_backlight=FF kpa_conf=21 ign_balance=00 als_retard_mintps=FF als_retard_maxtps=00 lcd_default_view=00 primary_trigger=01 secondary_trigger=02 tooth_wheel=23 trigger_tooth=00 another_trigger_tooth=09 crank_minper=4B tooth_wheel_twidth1=0A tooth_wheel_twidth2=0A cam_sync_r_edge_phase=01 cam_sync_f_edge_phase=02 reset_engphase_after=B4 ign_tdcdelay=B4 ign_dwell14=30 ign_dwell6=38 ign_crank_advance=28 ign_out=70 ignchmax=00 engine_off_delay=04 pump_on_mintime=06 fuelpump_channel=57 inj_stage2_rate=FF inj_stage2_start_tps=FF inj_stage2_start_map=FF als_deact_rpm=FF als_deact_time=00 als_deact_egt=00 als_retard=00 als_rev_limit=40 misc1out_minrpm=14 misc1out_maxrpm=FF misc1out_mintps=00 misc1out_maxtps=FF misc1out_minmap=91 misc1out_maxmap=FF misc1out_channel=B6 misc2out_minrpm=FF misc2out_maxrpm=FF misc2out_mintps=FF misc2out_maxtps=FF misc2out_minmap=FF misc2out_maxmap=FF misc2out_channel=FF act_wot_rpm=FF act_wot_channel=FF act_rpm_rpm=FF act_rpm_channel=FF egt1_cal=47 als_tks_channel=FF boost_conf=00 boost_targetoffs=00 boost_minpressure=FF boost_pid_kp=20 boost_pid_ki=80 boost_pid_kd=01 boost_pid_ilimit=FF boost_channel=FF water_pump_temp=00 hybrid_rpm_a=00 hybrid_rpm_m=00 water_pump_hyst=00 water_pump_channel=0F toothrel_normal=B5 toothrel_missing=76 fuelcut_min_kpa=12 fuelcut_max_kpa=FF tach_channel=FF tach_divider=FF shiftcut_conf=01 shiftcut_channel=FF shiftcut_time=00 softrpm_rpm=FF </code> '''09-08-06''' New Problem :-) Car starts directly but after few seconds dies. Checked everything and it's the rpm sensor (I'm using VR 36-1 Trigger wheel) at fault. Trying several sensors gave no solution. Rewired the sensor to no avail. * '''Do you have wheel error counts?''' ** Can you publish a datalog of it? Tim * Can you capture InputTrigger/TriggerLog to vrify VR sensor polarity ? Car ran perfect before this! Anybody any idea? Jochen, waar in belgiƫ woon je ergens, ik ben van begijnendijk, je kan me emailen op Tim.marteleur at regionaal.be Optional: Add document to category: Wiki formatting: * is Bullet list ** Bullet list subentry ... '''Bold''', ---- is horizontal ruler, <code> preformatted text... </code> See wiki editing HELP for tables and other formatting tips and tricks.