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IMPORTANT: enter the case-INsensitive alphabetic (no numbers) code AND WRITE SOME SHORT summary of changes (below) if you are saving changes. (not required for previewing changes). Wiki-spamming is not tolerated, will be removed, so it does NOT even show up in history. Spammers go away now. Visit Preferences to set your user name Summary of change: Installing Vems3.3 on a Volvo 244 with a B21ET engine. Taken out the dreadful K-jetronic to get complete control. This car should be competing this year in the Benelux Driftseries. My name is Jochen aka Brickdrifter and I'm living in Belgium. http://img273.imageshack.us/img273/9224/img86538ys.jpg '''2-09-06''' current setup: B21ET Ford brown top injectors Fuel pressure regulator (set to 2.5 bar) GrA 60/63 trim turbo XS Power intercooler Vems controls only injection! (for now) 36-1 trigger wheel with Ford VR sensor IAT sensor from webshop Volvo 960 TPS sensor 1.0.38 Firmware Megatune, no LCD :-( We will try to get the serial connections to work properly and download the actual firmware and config. Check groundconnections and achieve a triggerlog to analyse. Q: We have a problem getting the triggerlog with the terminalprogram.While cranking there is only weird characters spit out and no useful data. Maybe some wrong settings in Terminal? Here is the current config dump primep=00 primep_temp_scaling=80 cwl=B9 cwh=4B cranking_thres=03 awev=0A awev_temp_scaling=99 awec=2A warmup_clt_range[0]=00 warmup_clt_range[1]=00 warmup_clt_range[2]=00 warmup_clt_range[3]=14 warmup_clt_range[4]=50 warmup_clt_range[5]=64 warmup_clt_range[6]=78 warmup_clt_range[7]=8C warmup_clt_range[8]=AA warmup_clt_range[9]=C8 warmup_clt[0]=B4 warmup_clt[1]=AC warmup_clt[2]=AB warmup_clt[3]=AA warmup_clt[4]=A0 warmup_clt[5]=96 warmup_clt[6]=8A warmup_clt[7]=7A warmup_clt[8]=6E warmup_clt[9]=64 warmup_rpm_scale=BF req_fuel=2A divider=02 alternate=01 injopen=1F battfac=13 kpafac=96 kpaoffs=F6 injocfuel=20 injrampup_battfac=FF injpwm=33 injpwmt=FF injpwm6=33 rpmk[0]=0B rpmk[1]=B8 tpsdot_kpadot_conf=00 tpsdotrate[0]=06 tpsdotrate[1]=1A tpsdotrate[2]=66 tpsdotrate[3]=FF tpsaq[0]=19 tpsaq[1]=20 tpsaq[2]=2D tpsaq[3]=64 als_cut_mintps=FF tpsasync=06 acmult=00 tpsacold=78 launch_enrich=00 launch_retard=0D overrun_fuelcut=4D overrun_fuelresume=37 rev_limit=46 airden_ignore=00 config11=31 config12=40 config13=02 batt_cal=BD fastidle=C6 als_max_cut=00 dbaro=0C tps_low=26 tps_high=F5 fan_temp=00 fan_hyst=00 fan_channel=0F iac_step_seq=C9 iac_conf=40 iac_max_steps=FF iac_tps_thres=08 iac_cold_idle_temp=90 iac_warm_idle_temp=0C iac_cold_rpm=78 iac_warm_rpm=5C iac_cold_start_pos=E6 iac_warm_start_pos=D9 iac_afterstart_rpm=0F iac_afterstart_duration=96 iac_speed=32 iac_kp=14 iac_ki=0F iac_kd=1E launch_rpm=FF iac_integral_limit_dec=32 iac_integral_limit_inc=8C iac_integral_deadband=14 iac_deadband=0A als_cut_maxtps=00 iac_overclose_interval=80 iac_ref_pos[0]=BF iac_ref_pos[1]=B3 iac_ref_pos[2]=A6 iac_ref_pos[3]=99 iac_ref_pos[4]=8C iac_ref_pos[5]=80 iac_ref_pos[6]=73 iac_ref_pos[7]=66 iac_ref_pos[8]=59 iac_ref_pos[9]=4D iac_sol_channel=FF iac_ign_slope=20 softrpm_range=04 iac_ign_advance_limit=08 iac_ign_retard_limit=08 iac_ign_threshold=08 ego_conf=06 ego_lag=05 ego_coolant=B4 ego_maxtps=CC ego_maxmap=FF ego_minrpm=0C ego_maxrpm=28 ego_warmup=3C ego_lean_limit=26 ego_rich_limit=05 ego_pid_kp=28 als_enrich=00 ego_delta=33 ego_target=19 ego_pid_window=FF wbo2_warmup_ramp=C0 als_react_tps=00 wbo2_abs_limit=F5 wbo2_limit_maxt=A0 wbo2_fallback=60 wbo2_retry_t=06 wbo2_edgetime_corr=00 wbo2_edgetime_min=50 wbo2_ri_target=9A wbo2_nernstdc_target=89 wbo2_pump_pw_zero=64 wbo2_calibration=FE wbo2_heater_pid_kp=46 wbo2_heater_pid_ki=10 wbo2_heater_pid_kd=1A wbo2_heater_pid_ilimit=80 wbo2_pump_pid_kp=20 wbo2_pump_pid_ki=37 wbo2_pump_pid_kd=00 wbo2_pump_pid_ilimit=F5 wbo2_ri_confidence_scale=80 knock_conf=01 knock_sampling_window=FF knock1_frequency=29 knock1_gain=3F knock1_integrator=1F knock2_frequency=29 knock2_gain=3F knock2_integrator=1F knock_threshold=FF knock_noise_scale=FF knock_max_retard=00 knock_default_retard=00 knock_retard_step=00 knock_retard_delay=00 knock_advance_step=00 knock_advance_delay=00 knock_minrpm=FF knock_maxrpm=FF ve_learn_coolant=B4 ve_learn_max_power=FF ve_learn_rpm_scale=1E ve_learn_kpa_scale=1E ve_learn_ego_scale=43 ve_learn_min_weight=4D ve_learn_speed=FF ve_learn_limit=FF ve_learn_conf=00 lcd_c0=FE lcd_delay=FF lcd_backlight=FF kpa_conf=21 ign_balance=00 als_retard_mintps=FF als_retard_maxtps=00 lcd_default_view=00 primary_trigger=01 secondary_trigger=02 tooth_wheel=23 trigger_tooth=00 another_trigger_tooth=09 crank_minper=4B tooth_wheel_twidth1=0A tooth_wheel_twidth2=0A cam_sync_r_edge_phase=01 cam_sync_f_edge_phase=02 reset_engphase_after=B4 ign_tdcdelay=B4 ign_dwell14=30 ign_dwell6=38 ign_crank_advance=28 ign_out=70 ignchmax=00 engine_off_delay=04 pump_on_mintime=06 fuelpump_channel=57 inj_stage2_rate=FF inj_stage2_start_tps=FF inj_stage2_start_map=FF als_deact_rpm=FF als_deact_time=00 als_deact_egt=00 als_retard=00 als_rev_limit=40 misc1out_minrpm=14 misc1out_maxrpm=FF misc1out_mintps=00 misc1out_maxtps=FF misc1out_minmap=91 misc1out_maxmap=FF misc1out_channel=B6 misc2out_minrpm=FF misc2out_maxrpm=FF misc2out_mintps=FF misc2out_maxtps=FF misc2out_minmap=FF misc2out_maxmap=FF misc2out_channel=FF act_wot_rpm=FF act_wot_channel=FF act_rpm_rpm=FF act_rpm_channel=FF egt1_cal=47 als_tks_channel=FF boost_conf=00 boost_targetoffs=00 boost_minpressure=FF boost_pid_kp=20 boost_pid_ki=80 boost_pid_kd=01 boost_pid_ilimit=FF boost_channel=FF water_pump_temp=00 hybrid_rpm_a=00 hybrid_rpm_m=00 water_pump_hyst=00 water_pump_channel=0F toothrel_normal=B5 toothrel_missing=76 fuelcut_min_kpa=12 fuelcut_max_kpa=FF tach_channel=FF tach_divider=FF shiftcut_conf=01 shiftcut_channel=FF shiftcut_time=00 softrpm_rpm=FF '''09-08-06''' New Problem :-) Car starts directly but after few seconds dies. Checked everything and it's the rpm sensor (I'm using VR 36-1 Trigger wheel) at fault. Trying several sensors gave no solution. Rewired the sensor to no avail. * '''Do you have wheel error counts?''' ** Can you publish a datalog of it? Tim * Can you capture InputTrigger/TriggerLog to vrify VR sensor polarity ? Car ran perfect before this! Anybody any idea? Jochen, waar in belgiƫ woon je ergens, ik ben van begijnendijk, je kan me emailen op Tim.marteleur at regionaal.be Optional: Add document to category: Wiki formatting: * is Bullet list ** Bullet list subentry ... '''Bold''', ---- is horizontal ruler, <code> preformatted text... </code> See wiki editing HELP for tables and other formatting tips and tricks.