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IMPORTANT: enter the case-INsensitive alphabetic (no numbers) code AND WRITE SOME SHORT summary of changes (below) if you are saving changes. (not required for previewing changes). Wiki-spamming is not tolerated, will be removed, so it does NOT even show up in history. Spammers go away now. Visit Preferences to set your user name Summary of change: Audi A4 B5 (VW)VR6 12V 2.8 engine. Stock VR 60-2 trigger wheel in the crankcase. camsync=disabled "bosch motorsport" ignition coil continental flexfuel sensor connected to Whspeed1st. 4.9WBO 6pcs low-z injector, 8ch Active flyback. removable SD card, The battery (+) disconnected and shorted to GND before first cranking and startup. The HIFI audio system has had a big capacitor so it was discharged and sparked. After this the p259 chip has gone. There wasn't 5V on the lm1815 Pin8 and didn't read RPM signal. I changed the p259 chip, rpm shown, engine was started up. TDC_delay set up with strobe light, "Less tr. error" flag and missfire comes on 1800-2000rpm. VR sensor polarity was good, but tried to swap without result. Originaly r30=27K but after tried, 1K, 10K, 22K, 33K, and removed resistor(without pullup) without result, no different. Everytime got "tr error" around 2krpm. r181=150K originaly, I changed it to 270K, This was the only thing when i saw some change. The "tr error" came around 2300rpm. I kept the r181=270K and If i changed the r30 from 1k to 33K again. Without different. I tried to increase the r180 but the "tr error RPM edge come down". The best setup was: r30=22K, r180=270K. Originaly lm1815 pin5=4.95V, i jumpered it to 5V and changed the r30 from 1k to 33k again, No result. I tried to solder the ECU from VR to HALL as Marcel adviced, r30= 1K. Ec18/27 voltage = 2.40V, no rpm signal read when cranking. I tried the "Play trigger" tool but i saw trigger error and wrong rpm reading all the time. same on VR and HALL jumpered ECU Hw settings. Engine, body, battery and engine harness GND points checked and made to stronger. I tried to change the GND of the engine harness location from body to cylinder head, but no result again. Hard to check the trigger wheel runout because it's located in very bad position on the engine. This engine was running fine with another standalone ECU this before. Tried to lower the ignition dwell time from 3.01ms to 1ms maybe the coils makes electronic noises.... no result. I made new shielded cable separated from the harness, GNDed(shield, VR(-) ) everywhere, no different I didn't have scope. I would have made scopeshots if i would have had. I gave the ECU to Peter in baratka street to test. At first time we saw some weird RPM reading values.... need more testing. triggerlogs: http://www.vems.hu/files/Norbitron/v3.3_u014333-2018-01-26-09.39.36.triggerlog http://www.vems.hu/files/Norbitron/v3.3_u014333-2018-01-26-09.41.23.triggerlog Norbi Optional: Add document to category: Wiki formatting: * is Bullet list ** Bullet list subentry ... '''Bold''', ---- is horizontal ruler, <code> preformatted text... </code> See wiki editing HELP for tables and other formatting tips and tricks.